REALIZE THE FULL POTENTIAL OF EXISTING WELLS
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Candidate Evaluation and Selection
Design Optimization - Fluid selection | Chemistry Package
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Wellbore Cleanout
Treatment Delivery and Placement
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Selection and Design Optimization
Operation Execution
Value Based Performance
Production Recovery Increase
Return on Investment
Lost Production Recovery After Frac Hit
Case Study
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30-stage Mississippi Lime horizontal well experienced a severe frac hit following the completion of a nearby offset well.
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-40% EUR reduction due to frac hit from offset well
Initial attempts with wellbore cleanout and acid bullheading didn’t restore well performance
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Identified near-wellbore damage mechanism. Developed an optimized acid treatment strategy
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Deployed focused acid-treatment per stage
Treated all stages individually with 2,000 gals of acid
Performed entire operations on a single trip in just 24 hrs
Production Recovery Increase
Payout
IRR
EXPLORE MORE
ENGINEERING WORKFLOWS
Proven, Predictable, and Repeatable
EXCITE SYSTEMâ„¢
Delivers Reliable Operation Performance